[1]王南江,冯英,翁佳兴,等.微劈裂管路真空预压法加固深淤土地基应用研究[J].江苏水利,2016,(09):1-4,8.
 WANG Nanjiang,FENG Ying,WENG Jiaxing,et al.Application research of micro split pipeline vacuum preloading method in reinforcing deep silt soil foundation[J].JIANGSU WATER RESOURCES,2016,(09):1-4,8.
点击复制

微劈裂管路真空预压法加固深淤土地基应用研究()
分享到:

《江苏水利》[ISSN:1006-6977/CN:61-1281/TN]

卷:
期数:
2016年09期
页码:
1-4,8
栏目:
工程建设
出版日期:
2016-09-30

文章信息/Info

Title:
Application research of micro split pipeline vacuum preloading method in reinforcing deep silt soil foundation
文章编号:
1007-7839(2016)09-0001-04
作者:
王南江1冯英2翁佳兴3张礼强3
1.淮委治淮工程建设管理局,蚌埠 233000;
2.淮河水利水电开发公司(驻蚌)蚌埠 233000;
3.江苏鸿基水利建设工程有限公司,江苏 扬州 225000
Author(s):
WANG Nanjiang1 FENG Ying2 WENG Jiaxing3 ZHANG Liqiang3
1. Huaihe River Regulation Engineering Construction and Administration Bureau of Huaihe River Commission, Bengbu 233000, Anhui;
2. Huaihe Water Conservancy and Hydropower Development Company, Bengbu 233000, Anhui;
3. Jiangsu Hongji Water Conservancy Construction Engineering Co., Ltd, Yangzhou 225000, Jiangsu
关键词:
微劈裂管路真空预压堤基加固
Keywords:
micro split pipeline vacuum preloading foundation reinforcement
分类号:
TU443
文献标志码:
A
摘要:
短期内解决深淤土地基的沉降不稳定问题,是河道堤防工程施工过程中经常遇到的难题。本文介绍了微劈裂管路真空预压法在入江水道崇湾段堤基加固中的运用,通过在其南北凹两段布设真空度、地表沉降、地基承载力等监测设施,收集相关数据,并对监测数据进行了分析,结果表明该技术能有效降低上覆厚回填土层的影响,维持真空度在80~90 kPa,增压工艺能够较为显著提高地基的加固效果,技术实施75 d实现地基平均固结度大于90%,并且不同深度的地基承载力均可以达到设计要求。
Abstract:
Solving the settlement instability problem of the deep silt foundation in short term is a difficult problem during the construction of river embankment. The micro split pipeline vacuum preloading method used in the reinforcement of dike foundation of Chongwan section is introduced. The monitoring facilities are set up for collecting the data of vacuum degree, surface settlement and bearing capacity of foundation in the north and south concave. The monitoring data are analyzed.The results show that this technology can effectively reduce the influence of overlying thick backfill soil, maintain the vacuum degree in the 80 ~ 90 kPa. It can more significantly improve the reinforcement effect of foundation. The average consolidation degree of foundation is greater than 90% after technology implemented 75 days. The different depth of the foundation bearing capacity can meet the design requirements.

相似文献/References:

[1]龚丽飞,朱玲.真空预压处理新近吹填淤泥土设计与施工要点浅析[J].江苏水利,2015,(10):31.
[2]龚丽飞,朱玲.真空预压处理新近吹填淤泥土设计与施工要点浅析[J].江苏水利,2015,(11):31.
[3]宗 姗.淮河入江水道运河西堤崇湾段变真空预压排水固结技术试验研究[J].江苏水利,2016,(04):10.
 ZONG Shan.Experimental study on drainage consolidation technology with variable vacuum preloading at Chongwan section of Huaihe-into-Yangtze River watercourse[J].JIANGSU WATER RESOURCES,2016,(09):10.
[4]杨卫星,江季忠.南通市九圩港提水泵站工程 深基坑开挖及降水施工分析与探讨[J].江苏水利,2016,(07):5.
 YANG Weixing,JIANG Jizhong.Analysis and discussion on deep foundation pit excavation and dewatering construction of Jiuweigang pumping station project in Nantong[J].JIANGSU WATER RESOURCES,2016,(09):5.
[5]冯哲源,陶小玉,徐桂中,等.稻秸秆绳排水体真空固结处理高含水率疏浚淤泥可行性研究[J].江苏水利,2020,(07):56.
 FENG Zheyuan,TAO Xiaoyu,XU Guizhong,et al.Feasibility study on dredged silt with high moisture content treated by vacuum consolidation of straw rope drainage water body[J].JIANGSU WATER RESOURCES,2020,(09):56.
[6]王山,梁广雪,陈先勇,等.真空预压处理高含水率疏浚泥室内足尺大模型试验研究[J].江苏水利,2022,(12):1.
 WANG Shan,LIANG Guangxue,CHEN Xianyong,et al.Full-scale model test on dredged clay at high water content treated by vacuum preloading[J].JIANGSU WATER RESOURCES,2022,(09):1.

更新日期/Last Update: 2016-09-15